Friday, August 5, 2016

A LOT of unexpected Boat Work!


Its funny that the first date above, July 16 is Jane's birthday and the last date, August 5 is Sophia's birthday. Hopefully in our case the "old" will become "young" again. On Saturday the 16th we decided to take a spin into Narragansett bay to watch our yacht club's Regatta racing. Unfortunately half way out the starboard engine overheat alarm went off. It was exactly as it had happened on our sea trial in Maine on May 5. Jane shut down the starboard side but the port side did not seem to function so both were shut down as we floated in the bay to check out the engine room situation. There was no immediate evidence of something seriously wrong  so we crossed fingers and got the port engine started. This brought us almost back to Greenwich Bay and Peter tried the starboard engine again. It started and ran all the way back to the mooring. We thought it might be the solenoid, which was the explanation given to us on the sea trial. So it was on our calendar to have it looked at. On Sunday Jane decided to do some dusting in the aft cabin. Over the port side locker she discovered soot streaks on the white wall which were not there before. This finally explained the slight diesel smell we had ever since leaving Rockland, Maine. On further inspection some of Peter's clothes in his locker had soot on them and Jane discovered soot on the fitted sheet when she removed it from the bunk. So what we thought was diesel blow back was obviously a dangerous leak. The next day we had dePaul Diesel come over from Portsmouth to have a look. They confirmed the leak, showed us the rusty tube connections, took measurements,  and told us it had to be fixed asap.   To save some of the labor costs we started to get into the cupboards taking panels off, moving things out of the cabin and tried to find the exit point of the exhaust tubes. Both aft deck lazarettes were emptied to no avail so we took shelves and panels out of the aft cabin lockers. We could not find a visual sightline of the exhaust exit points. So, Peter had to cut away part of the walls in both aft lockers to finally find access. The mechanics actually found the exhaust tube split on the aft port side near the exit point.

This appeared after 2 months on the boat



After Jane left for the women's cruise on July 24,  Peter decided to have Kinvara II hauled out to have the exhaust work done. On the way across the bay the starboard engine  overheat alarm went off twice with the engine shutting down. This was concerning since Peter had to maneuver to fuel dock at NEB for pump out and the haul out dock by himself. Not an easy trip with only one engine working. After haul out the CAT mechanics took a look at the engines and discovered  that the raw water cooling system was not functioning well and could have caused the overheating and  hot exhaust making that system start to fail.

So Kinvara II has been on the hard since July 26. The exhaust system has been replaced. The raw water cooling systems were removed, acid dipped, and pressure tested. They are being reinstalled with new piping and  pump impellers. The mechanics told us it was a combination of age and low running  hours on the engine. These systems are supposed to be inspected either every 1000 hours or every 2 years, according to the manuels.  Hopefully we discovered the problems before any permanent engine damage has been done. On Monday or Tuesday we have a sea trial with the engine mechanic who will do a complete engine & exhaust survey.

We expected to have repairs and replacements over time with an older boat but to have two near catastrophic failures within 3 months of purchase came as a huge surprise, cost, and disappointment.
We had to cancel our visitors from North Carolina next week because we need to make sure all systems are working properly and safely before having people aboard again.

Same transmission cooler
after acid dip & cleaning


Starboard transmission cooler showing
almost complete blockage and orange silicone
where a rubber gasket should be.


Below are some pictures of 2 of the 6 coolers taken off the boat.
One of 4 engine thermostats showing
disintegrating rubber gasket and
evidence of silicone sealant, which should not have
been there
1 of 2 main engine coolers showing 50%
clogged with marine life. Accumulation of microscopic organisms
passing through filters over time

All coolers cleaned, pressure tested, sandblasted and painted.
Ready for re install and sea trial.



Peter used the time on the hard to scrape lots of marine growth off the propellers and shafts
and treat them with a spray paint to slow the growth. He also replaced the zincs which were
surprisingly very deterioated. We will have the bottom scraped by a diver
 before we head south in September.

Jane used the haul out time to do a little compounding and buffing
of the cabin top and trying to clean up the rust on the swim platform
supports and bolts.Before polishing....lots of rust!

After polishing.....nice and clean.


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